G9 Power

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  • Michael Eddie
    replied
    lol, I figured. Thanks for letting me know what the problem was

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  • ride65
    replied
    Drilled out the primary jet .004 runs great now. no choke needed, not even when cold.
    Don

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  • Michael Eddie
    replied
    You have to pull the clutch and side cover off and check the timing marks. Check the coil timing too on the flywheel side. The CDI box also controls the timing of the spark on the G9's so if you have somewhere you can swap one out to try it is worth a shot.

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  • ride65
    replied
    How do I check the timing? I can't find anything in the manual.(yamaha service manual)
    Don

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  • Michael Eddie
    replied
    Well, i might have to go with you on this now. How does the timing look?

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  • ride65
    replied
    checked the valves, on spec. bypassed the gov. now when you press the pedal to the floor it seems to have a miss. Back off then ease into it, the miss goes away when you reach crusing speed. choke dosen't affect miss
    Don

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  • ride65
    replied
    Mixture screw set at 1 1/2 turns, gaskets are new, will check valves

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  • Michael Eddie
    replied
    More touchy things on Yamaha's. Check the mix screw on the carburetor, about 1 1/2 turns out. Spark plug, all gaskets are good between the carburetor and the intake, gas is clean, valves could of been thrown out of adjustment but I would check that lastly if all else fails and there is nothing else to do.

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  • ride65
    replied
    I cleaned the carb and removed all the jets, cleaned them, and blew them out then checked the float adjustment, could the carb be jetted wrong?
    Updated by ride65; April 18, 2010, 07:08 PM.

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  • Michael Eddie
    replied
    Posted earlier by ride65 View Post
    the engine was gone thru about a year before I got it,oct 09, it actually looks like it, case gaskets, etc,(what you can see) the compression is 174, went thru the carb, & blew it out. trying to get hold of the guy that did the motor to find out exactly what he did. Would having the timing off by a tooth internally cause this ?
    If it was a timing problem it wouldn't run good at all. It could also be a clogged main jet on the carburetor, this is another problem using the choke fixes. So it might need a carb cleaning.

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  • ride65
    replied
    the engine was gone thru about a year before I got it,oct 09, it actually looks like it, case gaskets, etc,(what you can see) the compression is 174, went thru the carb, & blew it out. trying to get hold of the guy that did the motor to find out exactly what he did. Would having the timing off by a tooth internally cause this ?

    Leave a comment:


  • Michael Eddie
    replied
    The governor has nothing to do with the choke, so if you need to choke the cart to get it to go better up hills it might be about time for an engine rebuild. Rings, seals and crank seals.

    Leave a comment:


  • ride65
    started a topic G9 Power

    G9 Power

    I've got a G9 with problems going up hills. It seems that the gov. won't kick up the power a little use of the choke helps some but not alot. re-adjusted the entire throttle system from the pedal to the carb as per dealer manual. no leaks in the intake or crank seals (applied starting fluid to everything and didn't get a change in RPM) The gov shaft that goes into the trans seems to have a little slop. Any ideas would be appreciated
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